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滚筒加料机内壁粘料机理研究及其应用

Mechanisms of tobacco buildup on inner wall of casing cylinder and means of countermeasure

  • 摘要: 为解决卧式滚筒加料机内壁粘料问题, 引入赫兹-明德林黏附力模型, 构建了滚筒内壁粘料机理及“料幕”形成机理的简化力学模型, 推导出粘料条件与滑料/抛料运动微分方程。通过数值模拟, 分析了工艺参数对粘料条件及滑料/抛料运动轨迹的影响, 并运用计算流体力学方法模拟料液喷射雾化效果。结果表明: ①滚筒内烟叶颗粒的粘料现象与黏附力、静摩擦系数、滚筒转速及滚筒倾斜角等因素密切相关。②烟叶颗粒与滚筒之间的静摩擦系数和黏附力比值(烟叶颗粒与耙钉表面之间的黏附力/烟叶颗粒与滚筒内壁之间的黏附力)对烟叶颗粒粘附时所需最小黏附力的影响显著, 滚筒转速对抛料轨迹的影响较大。③当料液黏度由0.001 kg/ms随机调整并增加到0.700 kg/ms时, 料液颗粒轨迹及质量分数分布基本保持不变, 但料液颗粒平均粒径减小。④通过对喷嘴参数的调整, 粘料量降低至≤0.32 kg/批。该研究成果有助于卷烟厂降低物料损耗并提高生产效率。

     

    Abstract: To prevent tobacco buildup on the inner wall of a horizontal casing cylinder, the Hertz-Mindlin adhesion force model was introduced and simplified mechanical models were established for the tobacco adhesion phenomenon on the cylinder wall and the formation mechanism of the tobacco curtain inside the cylinder. Differential equations were also derived for the adhesion conditions and sliding/projecting movement of tobacco particles. Numerical simulations were conducted to analyze the impact of process parameters on tobacco adhesion conditions and the trajectories of tobacco sliding and projecting movement. Additionally, the atomization effects of casing spraying were simulated using the computational fluid dynamics (CFD) method. The results showed that: 1) The adhesion of tobacco particles to the inner wall of the cylinder was closely correlated with factors such as the adhesive force, the static friction coefficient, and the rotational speed and inclination angle of the cylinder. 2) The static friction coefficient between tobacco particles and the cylinder, as well as the ratio of the adhesive force between a tobacco particle and the spiker surface versus that between a tobacco particle and the inner wall of the cylinder, significantly affected the minimum adhesive force required for tobacco particle adhesion. Meanwhile, the rotational speed of the cylinder substantially impacted the projecting trajectory of tobacco particles. 3) When the viscosity of the casing was randomly adjusted and increased from 0.001 to 0.700 kg/ms, the trajectory and mass fraction distribution of casing particles remained basically unchanged, though the average particle size of the casing decreased. 4) By adjusting the casing nozzle parameters, the amount of tobacco buildup on the inner wall of the cylinder could be reduced to ≤0.32 kg per batch. The findings in this research aid cigarette factories to reduce material loss and improve production efficiency.

     

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